“Jim, we got a heartbeat!” – Leonard McCoy
The roto-tiller is fixed. Finally. I woke up yesterday morning at 6 am and just couldn’t get back to sleep, so I decided to stay up. After going downstairs, puttering a little bit, fed the cat and finished a blog entry, I checked the weather for Thursday and noted that it was fairly chilly outside for a mid-June morning. Something sort of called me out to the garage, so I went out there and stared at a few things before my eyes fell on the half-fixed roto-tiller. I decided then and there that it was going to get finished. It was only a fuel line connection to the gas tank (and a fuel filter installation) away from being done.
The gas tank was still off, so I had to finish putting on one of the small covers that prevents dirt from getting into the starter cord holder. The nut only barely went on the bolt so I was forced to do a little finagling with a wrench and my drill/driver, but I finally got it back on. Screwed in the self-tapping screw at the top and I was ready to go on to the gas tank. Which turned out to be fairly easy, since the rust patterns on the various pieces reminded me of where they went. Put the bolts in the respective holes, lined up the rust patterns and in this case used my impact driver to drive them in securely.
I had purchased a new spark plug, so I put that in after checking to be sure the gap was correct. At that point I ran into a little snag with the fuel line, but a bit of measuring along with a couple of mishaps, and I was glad I had purchased the longer length of hose, as I ended up needing almost all of it to get it all connected, since I measured wrong the first time. But after getting it all figured out, clamped up, I kneeled back and gave myself a little greasy pat on the back. Checked my work to be sure I didn’t have any parts left over (didn’t!) and then went to get the gas can. I filled the gas tank a little, checked to be sure there wasn’t a leak anywhere (yay, no!) and then filled the tank about halfway.
Moment of truth. I checked the choke on the carb, and pulled the starter cord. Nothing. Looked up at the controls and realized the lever was still set at ‘STOP’. Duh! I pushed the lever forward to ‘START’ and then pulled the starter cord again. Still nothing. On the third pull, I was rewarded with a chug and the engine caught. Apparently the complete lack of fuel in the system caused it to need a bit more in the carb to get things going. But once the engine caught it continued to run, but it was running a little roughly. I switched up the lever a bit more and it started to run a bit more smoothly. But the governor was still surging a little, so I tweaked the carb until it evened out. Once that was done, I revved the engine a little bit to find where the various speeds needed to be. After doing that, I wound it down a bit, and then pulled the lever all the way back to stop. Contrary to what it had been doing, where in order to stop I needed to pull the connector off the spark plug, this time the engine wound down on its own and stopped finally.
At this point I decided to take it outside the garage and give it a little test under load, where pre-repair it was having the most trouble. Bringing it out beside the garage, I drove it into a patch of ground that had been tilled about a two weeks ago, when I was in the middle of trying to repair the old carb and had it all together and trying to see what it would do. This time when I put it into gear, the engine didn’t die down or ‘hunt’ when the tines bit into the earth, it stayed high in the RPMs and cut through the ground like it was nothing. Even moving into a patch that hadn’t been tilled before caused the same result, it worked just like there was nothing amiss. Success! Not wanting to wake the entire neighborhood (the engine on the tiller is a little loud, I’ve taken to wearing hearing protection while running it) I brought it back into the garage and shut it down.
This project has taken me I think the better part of a month to complete, but it hasn’t been without merit. I think I’m perfectly capable of effecting successful repairs on it should the need arise, given my experience and that should save me money in the long run. If nothing else I have considerable documentation, pictures and having documented my efforts here and elsewhere (I kept notes) it should keep me from having to find someone else to do the work for me. Certainly I can change the oil myself now, and that’s a big thing when it comes to swapping out equipment for the changing seasons. And I can take the knowledge of this and apply it to my snowblower, since the engines are nearly identical. So bonus for that too.
It runs! It’s fixed! Now I have to move on to the desktop computer. Go me!